The bronze bearing was fabricated on a lathe. A through hole was drilled concentric to the outer diameter of a bronze rod. The end of the rod was beveled to allow it to be pressed into the N hole mentioned above. A small seat was made with an end mill to house the tiny o-ring which sealed the motor shaft from water. The rod was then parted to make the bearing.
Finally, an impeller was fabricated on a Makerbot 3D printer from a design I created in Solidworks. The impeller is not anything fancy, and is not optimized at all. Part of the point of this project for students is to design their own impellers and then to test the efficiency of the pump. Nevertheless, the pump worked when I tested it (at least as soon as i figured out which side was the inlet and outlet).
In the video below, you can see that the pump can supply a limited amount of potential energy; as the outlet tube is raised, the flow rate diminishes until its maximum pumping height is reached where the flow rate is zero.
In the video below, you can see that the pump can supply a limited amount of potential energy; as the outlet tube is raised, the flow rate diminishes until its maximum pumping height is reached where the flow rate is zero.